Part 21 Report - 1998-241

ACCESSION #: 9803040105 LICENSEE EVENT REPORT (LER) FACILITY NAME: Clinton Power Station PAGE: 1 OF 6 DOCKET NUMBER: 05000461 TITLE: Division 2 Nuclear Systems Protection System Inverter Not in Accordance With the Plant's Design Basis Due to Various Deficiencies EVENT DATE: 01/27/98 LER #: 98-004-00 REPORT DATE: 02/26/98 OTHER FACILITIES INVOLVED: None DOCKET NO: 05000 OPERATING MODE: 4 POWER LEVEL: 000 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR SECTION: 50.73(a)(2)(ii) LICENSEE CONTACT FOR THIS LER: NAME: M.D. Wagner, System Engineer TELEPHONE: (217) 935-8881 Extension 4071 COMPONENT FAILURE DESCRIPTION: CAUSE: X SYSTEM: EF COMPONENT: INVT MANUFACTURER: E209 REPORTABLE NPRDS: Y SUPPLEMENTAL REPORT EXPECTED: YES EXPECTED SUBMISSION DATE: 05/08/98 ABSTRACT: With the plant in COLD SHUTDOWN technicians identified various deficiencies in the installed Silicon Controlled Rectifiers (SCR) and power diodes of the Division 2 Nuclear Systems Protection System (NSPS) inverter. The compressive force applied to the heatsink clamp hardware for SCRs and power diodes had been applied and verified incorrectly causing loose connections. Therefore, the inverter likely would not have been capable of performing its safety function during a seismic event. Miscalibration of the inverter lock-up detector assembly resulted in a loss of the simulated inverter loads during testing under inverter full load conditions, whereby loss of the simulated bypass power test source resulted in a reverse transfer of the inverter to the missing bypass power test source, and a loss of power to the simulated inverter load bank. These conditions are not in accordance with the plant's design basis. A cause evaluation for this event has not been completed and corrective actions have not been identified. However, the Division 2 NSPS inverter SCR and power diode installations have been corrected and other inverters will be inspected for similar deficiencies and corrected. This event is also reportable under 10CFR21. END OF ABSTRACT TEXT PAGE 2 OF 6 DESCRIPTION OF EVENT On December 25, 1997, the plant was in Mode 4 (COLD SHUTDOWN) for the six Outage (RF-6), and reactor (RCT) coolant temperature was being maintained within a band of 95 to 115 degrees Fahrenheit (F) and pressure was zero pounds per square inch. At about 1245 hours, operators in the Main Control Room (MCR) received an unexpected alarm indicating that the Nuclear Systems Protection System (NSPS) [EF] inverter [INVT), 1C71-S001B, automatically transferred from its normal power source to its alternate source. At 1246 hours, an area operator verified that the Division 2 NSPS inverter was on the alternate power source. Electrical Maintenance technicians were dispatched to the inverter, and Maintenance Work Request (MWR) D79429 was initiated to investigate the automatic transfer. Four uninterruptible NSPS buses (BU) supply Class 1E 120 Volts Alternating Current (AC) power to the four logic divisions of the Reactor Protection System [JC]. An NSPS bus is normally fed via a Direct Current (DC) to AC inverter supply. The inverter is fed by a 125 Volts DC divisional battery charger [BYC] with a floating battery [BTRY]. In the unlikely event of an inverter failure/power loss, the NSPS bus automatically transfers via a solid state transfer switch, to an alternate 120 Volts AC source derived from a 480 Volts AC to 120 Volts AC transformer [XFMR] supply. Also, 120 Volts AC can be supplied to the Division A and B NSPS buses by manual transfer to an inverter maintenance bypass feed. On January 7, 1998, during performance of MWR D79429, technicians identified several deficiencies in the installed Silicon Controlled Rectifiers (SCR) and power diodes of the Division 2 NSPS inverter. The deficiencies included: SCR gate and cathode leads were not tightly twisted, making the inverter more susceptible to electrical noise from outside sources; SCRs and power diodes had evidence of arcing on the conducting surface of the devices, indicating that these devices had degraded electrical continuity; and excessive Wakefield heat transfer compound was found applied to the conductive surfaces of the SCRs and power diodes, creating the potential for hot spots and long term degradation of the SCRS, power diodes, and the inverter. Technicians also identified that SCRs had dimples on their conductive surfaces from the SCR heatsink clamp alignment pin impinging on the SCR surface due to the SCRs not being properly centered during previous installations of the SCRs, and additional mechanical defects were noted on SCRs and power diodes which did not appear to be directly related to the alignment pin dimples. These conditions affect the conductive surfaces of the semi-conductors, thereby degrading electrical continuity. In addition, the compressive force applied to the heatsink clamp hardware (General Electric Press Pac Clamp Assembly) during previous installations of SCRs and power diodes had been applied and verified incorrectly using a torque value. The application of excessive force caused the Press Pac spring bars to flex beyond their yield point, resulting in inadequate compressive force applied to the installed SCRs and power diodes. One semiconductor assembly was installed in an incorrect order, resulting in the device being out of position with regards to the compression centering plates. This condition degraded electrical continuity because the centering pins were not in the proper position. TEXT PAGE 3 OF 6 Electrical testing of the improperly installed SCRs and power diodes in the Division 2 NSPS inverter during performance of MWR D79429 indicated that immediate failure of the these Components was not likely and immediate operability of the inverter was not affected by the deficiencies described above. The improper installation of devices described above can result in increased heating and arcing of the affected devices and long term degradation of the semi-conductors. The impact of improper twisting of SCR gate and cathode wires is somewhat mitigated by plant procedures which control the likely outside sources of electrical noise. The improper compressive force on SCRs and power diodes may cause premature degradation of the SCRs, thereby creating the potential for the inverter to not operate as designed. Condition Report 1-98-01-066 wag initiated to track an investigation land resolution for these issues. MWRs were initiated to inspect other potentially affected equipment including the Division 1 NSPS inverter, 1C71-S001A, the Division 3 NSPS inverter, 1C71-S001C, the Division 4 NSPS inverter, 1C71-S001D, the A NSPS Solenoid(RPS) Uninterruptible Power supply (UPS) Inverter, 1C71-S004A, and the B NSPS Solenoid (RPS) UPS Inverter, 1C71-S004B, On January 12, 1998, during performance of KWR D79429 on the Division 2 inverter, technicians noted that the bolts in the Press Pac spring bar (General Electric Press Pac Clamp Assembly) used to determine the amount of force being applied to the SCRs and power diodes felt loose although the Press Pac spring bar was indicating the proper compressive force. Investigation of this issue identified that the Press Pac spring bar was bent, resulting in less than the required compressive force being applied to the SCRs and power diodes. CR 1-98-01-137 was Initiated to track an investigation and resolution for these issues. The Operations Shift Supervisor made resolving this issue a restraint to changing reactor modes. This issue also potentially affects the Divisions 1, 3, 4, NSPS inverters, and the A and B NSPS Solenoid (RPS) UPS inverters. On January 27, 1998, during evaluation of the inadequate compressive force issue as documented in CR 1-98-01-137, the system engineer concluded that torquing the General Electric Press Pac Clamp Assembly to 90 to 100 inch pounds caused the Press Pac spring bar to bend beyond its designed limit, resulting In improper compressive force on the SCRs and power diodes, and loose connections and arcing on the semi-conductor surfaces. As a result of the bent Press Pac spring bar and loose connections, the inverter likely would not have been capable of performing its intended safety function during a seismic event. Therefore, the Division 2 NSPS inverter was not in accordance with the plant's design basis. On February 1, 1998, during performance testing of the Division 2 NSPS inverter in accordance with MWR 079429, technicians reported that a loss of the simulated bypass power test source under inverter full load conditions (while on a resistive load bank) resulted in a reverse transfer of the inverter to the bypass power test source (which was intentionally de-energized as part of the test procedure). The reverse transfer resulted in a loss of power to the simulated inverter load bank. This condition is not in accordance with the plant's design basis. However, this condition did not exist at lower test loads which are more representative of actual inverter load conditions. TEXT PAGE 4 OF 6 Investigation of the reverse transfer issue with the inverter supplier identified that the deficiency is the result of improper calibration of the lock-up detector adjustment. The improper calibration was performed in accordance with maintenance procedure CPS 8503.03, "NSPS Inverter Calibration." CR 1-98-01-455 was initiated to track an investigation and resolution for these issues. This issue also potentially affects the Divisions 1, 3, 4, NSPS inverter, and the A and B NSPS Solenoid (RPS) UPS inverters. No automatic or manually initiated safety system responses were necessary to place the plant in a safe and stable condition. This event was not directly affected by other inoperable equipment or components. CAUSE OF EVENT Illinois Power (IP) has determined that incorrect guidance was being used for installing the Press Pac spring bar and calibrating the inverter lock-up detector adjustment. A record of coordination between IP and the inverter supplier, dated August 4, 1988, and contained in vendor manual X2801-0144, provided the incorrect method of applying compressive force using a torque value. Recent guidance from the inverter supplier recommends not using torque as the means for verifying the compressive force applied to the SCRs and power diodes installed in the heatsinks. The current supplier-recommended method of applying and verifying compressive force applied to the SCR and power diode surfaces uses a gauge and visual indication of a Press Pac spring bar. IP expects to submit a supplemental report identifying the cause, corrective action, assessment of the safety consequences and implications, and similar event information for this event by May 8, 1998. CORRECTIVE ACTION CorrectIve action for this event has not been identified, pending completion of the cause evaluation. The bent Press Pac spring bar has been replaced and proper compressive force has been applied to the SCRs and power diodes in the Division 2 NSPS inverter in accordance with MWR D79429. IP will inspect the Divisions 1, 3, and 4 NSPS inverters and the A and B NSPS Solenoid (RPS) UPS inverters for deficiencies similar to those described in this report and correct identified deficiencies, as necessary, to ensure the equipment is capable of performing their intended safety functions. ANALYSIS OF EVENT This event is reportable under the provisions of 10CFR50.73 (a) (2) (ii) (B) because the Division 2 inverter was not in accordance with the design basis of the plant An assessment of the safety consequences and implications associated with this event has not bean completed but will be provided in a supplement to this report. TEXT PAGE 5 OF 6 ADDITIONAL INFORMATION The Divisions 1, 2, 3, and 4 NSPS inverters are model number INV-752-1- 101, manufactured by Elgar Corporation. The A and B NSPS Solenoid (RPS) inverters are model number UPS-102-1-189, manufactured by Elgar Corporation. Previous similar event information will be provided in a supplement to this report. For further information regarding this event, contact M. D. Wagner, System Engineer, at (217) 935-8881, extension 4071. IP is providing the following information in accordance with 10CFR21.21(d)(4). Initial notification of this matter will be provided by facsimile of the letter to the NRC Operations Center in accordance with 10CFR21.21(d)(3) within two days of the date the responsible officer signs this letter. (i) Walter G. MacFarland, Chief Nuclear Officer of IP, Clinton Power Station, Highway 54, 6 Miles East, Clinton, Illinois, 61727, is informing the Nuclear Regulatory Commission of a condition reportable under the provisions of 10CFR, Part 21. (ii) The basic component involved in this condition is the safety- related Division 2 NSPS inverter, manufacturer model number INV-752-1-101. (iii) The Division 2 NSPS inverter was supplied to Clinton Power Station by Elgar Corporation. (iv) During troubleshooting of the Division 2 NSPS inverter on January 12, 1998, IP noted that the bolts in the Press Pac spring bar (General Electric Press Pac Clamp Assembly) used to determine the amount of force being applied to the SCRs and power diodes felt loose although the Press Pac spring bar was indicating the proper compressive force. Investigation of this issue identified that the Press Pac spring bar was bent, resulting in less than the required compressive force being applied to the SCRs and power diodes. On January 27, 1998, during evaluation of the inadequate compressive force issue, IP concluded that torquing the General Electric Press Pac Clamp Assembly to 90 to 100 inch pounds caused the Press Pac spring bar to flex beyond its yield point, resulting in inadequate compressive force on the SCRs and power diodes, and loose connections and arcing on the semi-conductor surfaces. As a result of the bent Press Pac spring bar and loose connections, the inverter likely would not have been capable of performing its intended safety function during a seismic event. The safety function of the Division 2 NSPS inverter is to supply uninterruptible NSPS buses with Class 1E 120 Volts AC power for the Division 2 logic of the Reactor Protection System. Therefore, the Division 2 NSPS inverter was not in accordance with the plant's design basis. TEXT PAGE 6 OF 6 Illinois Power has determined that the inverter supplier provided incorrect guidance for Installing the Press Pac spring bar. A record of coordination between IP and the inverter supplier, dated August 4, 1988, and contained in vendor manual K2801-0144, provided the incorrect method of applying compressive force using a torque value. Recent guidance from the inverter supplier recommends not using torque as the means for verifying the compressive force applied to the semi-conductor devices installed in the heatsinks. The current supplier-recommended method of applying and verifying compressive force applied to, the semi-conductor surfaces uses visual indication of a Press Pac spring bar. On February 1, 1998, during performance testing of the Division 2 NSPS inverter in accordance with MWR D79429, technicians reported that a lose of the simulated bypass power test source under inverter full load conditions (while on a resistive load bank) resulted in a reverse transfer of the inverter to the missing bypass power test source. The reverse transfer resulted in a lose of power to the simulated inverter load bank. This condition is not in accordance with the plant's design basis. However, this condition did not exist at lower test loads which are more representative of actual inverter load conditions. Investigation of the reverse transfer issue with the inverter supplier identified that the deficiency is the result of improper calibration of the lock-up detector adjustment. The improper calibration was performed in accordance with maintenance procedure CPS 8503.03, "NSPS inverter Calibration." Illinois Power has determined that the inverter supplier had not provided proper guidance for calibrating the inverter lock-up detector adjustment. (v) The incorrect application and verification methods for applying compressive force to SCRs and power diodes was identified on January 7, 1997, and determined to be potentially reportable under 10CFR21. On January 12, 1993, a bent Press Pac spring bar was identified on the Division 2 NSPS inverter. The incorrect calibration of the Division 2 NSPS inverter was identified on February 1, 1998 and determined to be potentially reportable under 10CFR21. (vi) CPS has six safety-related inverters that may be affected by these deficiencies, including the Division 1 NSPS inverter, 1C71-S001A, Division 2 NSPS inverter, 1C71-S001B, the Division 3 NSPS inverter, 1C71-S001C, the Division 4 NSPS inverter, 1C71-S001D, the A NSPS Solenoid (RPS) UPS Inverter, 1C71-S004A and the B NSPS Solenoid (RPS) UPS Inverter, 1C71-5004B. IP is not aware of other facilities that could be affected by this deficiency. (vii) Corrective action for this issue has not been identified, pending completion of the cause evaluation. However, some currently identified actions are discussed in the LER CORRECTIVE ACTION section of this report. (viii) IP has no advice for other purchasers or licensees regarding this issue. ATTACHMENT TO 9803040105 PAGE 1 OF 1 POWER REACTOR EVENT NUMBER: 33800 FACILITY: CLINTON REGION: 3 NOTIFICATION DATE: 02/26/98 UNIT: [1] [ ] [ ] STATE: IL NOTIFICATION TIME: 16:18 [ET] RX TYPE: [1] GE-6 EVENT DATE: 02/26/98 EVENT TIME: 16:18 [CST) NRC NOTIFIED BY: R. FRANTZ LAST UPDATE DATE: 02/26/98 HQ OPS OFFICER: JOHN MacKINNON NOTIFICATIONS EMERGENCY CLASS: NOT APPLICABLE 10 CFR SECTION: JEFF WRIGHT RDO CDEG 21.21(c)(3)(i) DEFECTS/NONCOMPLIANCE VERN HODGE (PCEB) NRR UNIT SCRAM CODE RX CRIT INIT PWR INIT RX MODE 1 N N 0 COLD SHUTDOWN CURR PWR CURR RX MODE 0 COLD SHUTDOWN EVENT TEXT DIVISION 2 NUCLEAR SYSTEMS PROTECTION SYSTEM INVERTER NOT IN ACCORDANCE WITH THE PLANT'S DESIGN BASIS DUE TO VARIOUS DEFICIENCIES. WITH THE PLANT IN COLD SHUTDOWN, PLANT TECHNICIANS IDENTIFIED VARIOUS DEFICIENCIES IN THE INSTALLED SILICON CONTROLLED RECTIFIERS (SCR) AND POWER DIODES OF THE DIVISION 2 NUCLEAR SYSTEMS PROTECTION SYSTEM (NSPS) INVERTER. THE COMPRESSIVE FORCE APPLIED TO THE HEAT SINK CLAMP HARDWARE FOR SCRs AND POWER DIODES HAD BEEN APPLIED AND VERIFIED INCORRECTLY CAUSING LOOSE CONNECTIONS. THEREFORE, THE INVERTER LIKELY WOULD NOT HAVE BEEN CAPABLE OF PERFORMING ITS SAFETY FUNCTION DURING A SEISMIC EVENT. MISCALIBRATION OF THE INVERTER LOCK-UP DETECTOR ASSEMBLY RESULTED IN A LOSS OF THE SIMULATED INVERTER LOADS DURING TESTING UNDER INVERTER FULL LOAD CONDITIONS, WHEREBY LOSS OF THE SIMULATED BYPASS POWER TEST SOURCE RESULTED IN A REVERSE TRANSFER OF THE INVERTER TO THE MISSING BYPASS POWER TEST SOURCE, AND A LOSS OF POWER TO THE SIMULATED INVERTER LOAD BANK. THESE CONDITIONS ARE NOT IN ACCORDANCE WITH THE PLANT'S DESIGN BASIS. A CAUSE EVALUATION FOR THIS EVENT HAS NOT BEEN COMPLETED AND CORRECTIVE ACTIONS HAVE NOT BEEN IDENTIFIED. HOWEVER, THE DIVISION 2 NSPS INVERTER SCR AND POWER DIODE INSTALLATION HAVE BEEN CORRECTED AND OTHER INVERTERS WILL BE INSPECTED FOR SIMILAR DEFICIENCIES AND CORRECTED. *** END OF DOCUMENT ***

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