Part 21 Report - 1999-211

ACCESSION #: 9903310302


Table of Contents


LICENSEE EVENT REPORT (LER)
FACILITY NAME: R. E. Ginna Power Plant PAGE: 1 OF 7
DOCKET NUMBER: 05000244
TITLE: Deficiencies in NSSS Vendor Steamline Break Mass & Energy Release Analysis results in Plant Being Outside its Design Basis
EVENT DATE: 02/22/1999 LER #: 1999-001-00 REPORT DATE: 03/24/1999
OTHER FACILITIES INVOLVED: DOCKET NO: 05000
OPERATING MODE: 1 POWER LEVEL: 75
THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR SECTION: 50-73(a)(2)(ii)
Part 21
LICENSEE CONTACT FOR THIS LER:
NAME: John St. Martin - Technical Assistant TELEPHONE: (716) 771-3641
COMPONENT FAILURE DESCRIPTION:
CAUSE: SYSTEM: COMPONENT: MANUFACTURER:
REPORTABLE EPIX:
SUPPLEMENTAL REPORT EXPECTED: YES

ABSTRACT:

On February 22, 1999, Ginna Station was notified by its NSSS vendor (Westinghouse) of two modeling errors in the analysis for a main steamline break inside containment with an assumed single failure of a main feedwater regulating valve. These errors had a nonconservative impact on calculated peak containment pressure.

The first error involved the omission of a previously unaccounted for volume of high temperature feedwater. The second error resulted in an incorrect feedwater isolation time.

The consequences of these two modeling errors has the potential for containment to exceed its design basis value of 60 psig for a main steamline break with a concurrent failure of a main feedwater regulating valve.

The cause of the plant being in a condition that was outside the design basis of the plant was deficiencies in the Westinghouse main steamline break mass and energy release analysis.

Immediate corrective action was to place a temporary administrative restriction of 40 degrees Fahrenheit maximum on screenhouse bay temperature, a measure of Service Water/Containment fan cooler heat removal and pressure reduction capability, for Modes 1 through 4 (when containment is required to be operable) to ensure adequate post-accident environmental conditions margin existed.

Corrective action to prevent recurrence is outlined in Section V.B. Additional corrective actions, if needed, will be identified in a supplement to this LER.


I. PRE-EVENT PLANT CONDITIONS:

In 1992, the NSSS vendor for Ginna Station (Westinghouse) analyzed a full spectrum of cases for the main steam line break (MSLB) and containment response for the R. E. Ginna plant. The set of analyses was performed to support the program to reduce the boric acid storage tank (BAST) boron concentration to 2000 ppm. This analysis entailed over 120 cases, which varied break size and location, initial power level, single failure, offsite power availability, and different reactivity coefficients (rodded versus unrodded). In 1995, Westinghouse re-visited the steamline break mass and energy release event due to replacement steam generators (RSGs) and an increase to 18 month fuel cycles. Many of the previous cases could be eliminated due to:

1. An integral flow restrictor on the RSGs, eliminating any breaks larger than 1.4 square feet (the RSGs have flow restricting outlet nozzles which make any break size larger than the throat area of the restrictor not credible and thus, break flow areas greater than 1.4 square feet no longer need to be considered), and

2. Credit being taken for the main steam non-return check valve, which eliminated several types of breaks and the need to consider a main steam isolation valve (MSIV) single failure for containment overpressurization cases.

After eliminating cases that were no longer credible, cases for the 1995 analyses were selected from the 1992 BAST reduction program. Six of the most limiting cases were selected,including different break sizes, initial power levels, single failures, and offsite power assumptions. Another difference from the previous analyses is explained in the Ginna Station Updated Final Safety Analysis Report (UFSAR) Section 6.2.1.2.3:

"In the Reference 3 analyses [1992 BAST reduction program], the most limiting feedwater control system failure was assumed to be a failure in the auxiliary feedwater system control. This failure resulted in increased auxiliary feedwater flow rates for the entire duration of the transient. A failure of the isolation function of the main feedwater regulating valves (MFRVs) was not considered because a feedwater isolation signal also results in a main feedwater pump trip and in closure of the pump discharge valve (MFPDV). Thus, no single failure would have resulted in a failure to isolate main feedwater or a significant delay in the isolation of main feedwater to the affected steam generator. It has subsequently been realized that the condensate pumps would continue to pump through the main feedwater pumps at low steam generator pressures and that the pump discharge (MFPDV) closure time is approximately 80 seconds. Therefore, a failure of the isolation function of the main feedwater regulating valve (MFRV) could result in main feedwater flow via the condensate pumps for approximately 80 seconds to the affected steam generator. This new failure scenario is a more limiting failure than was assumed in the previous analyses due to the timing and magnitude of the increased flow."

The requirement to maintain operability of the main steam non-return check valves and the 80 second stroke time requirement of the MFPDV is addressed in the Ginna Station Improved Technical Specifications (ITS) Sections 3.7.2 and 3.7.3 respectively.

II. DESCRIPTION OF EVENT:

A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:

February 22, 1999: Event date.

February 22, 1999, 1540 EST: Discovery date and time.

February 22, 1999, 1601 EST: NRC is notified of this condition per 10CFR50.72 (b) (1) (ii) (B).

March 1, 1999, 2018 EST: Plant is shutdown in Mode 4 for the planned 1999 refueling outage.

B. EVENT:

On February 22, 1999, in activities unrelated to plant conditions, Ginna Station was notified by its NSSS vendor (Westinghouse) of two modeling errors in the analysis for a MSLB inside containment with an assumed single failure of a MFRV. (Refer to the letter RGE-99-207 from Mr. Steve M. Ira of the Westinghouse Electric Corporation to

Mr. Peter Bamford, Rochester Gas and Electric Corporation (RG&E), dated February 22, 1999, Subject: Steamline Break Mass and Energy Release Analysis Nonconformance.) These errors had a nonconservative impact on calculated peak containment pressure. The first error involves the volume of feedwater that exists between the specified isolation valve and the faulted steam generator. When the MFRV is assumed to fail to perform its isolation function, then the isolation function is performed by the MFPDV. Because of the relative locations of these valves to the steam generator, the volume of water is greater between the MFPDV and the steam generator than between the MFRV and the steam generator. This increased volume of high temperature feedwater was not accounted for in the analysis.

The second error was inadvertently isolating feedwater flow at 15 seconds instead of at 85 seconds (80 seconds valve stroke time and 5 seconds for signal delay) as was intended. This meant that feedwater flow should have continued for 70 seconds longer than was assumed in the analysis.

The consequences of these two modeling errors has the potential for containment to exceed its design basis value of 60 psig for a MSLB with an assumed concurrent failure of a MFRV. This is due to adding higher energy fluid to containment for 70 seconds longer than was assumed in the 1995 MSLB analysis of record. There was also the potential for the containment to exceed its design basis value as documented in the 1992 analyses, due to discovery of a more limiting single failure.

At the time of discovery and until the planned shutdown on March 1, 1999, the screenhouse bay temperature was maintained at approximately 39 degrees Fahrenheit, while lake temperature remained at approximately 35 degrees Fahrenheit. Ginna Station placed a temporary administrative restriction of 40 degrees Fahrenheit maximum on screenhouse bay temperature, a measure of Service Water System temperature, for Modes 1 through 4 (when containment is required to be operable). By maintaining this cooling medium for the containment fan coolers at such a low temperature, increased containment fan cooler heat removal ability was ensured and this, combined with a high cycle-specific excess shutdown margin, was sufficient to ensure containment pressure would remain less than 60 psig for this postulated scenario.

C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None

D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None

METHOD OF DISCOVERY:

This event was disclosed to RG&E by the notification from its NSSS vendor (Westinghouse) of two modeling errors in the analysis for a MSLB inside containment with an assumed single failure of a MFRV. (Refer to letter RGE-99-207 from Mr. Steve M. Ira of the Westinghouse Electric Corporation to Mr. Peter Bamford, Rochester Gas and Electric Corporation (RG&E), dated February 22, 1999, Subject: Steamline Break Mass and Energy Release Analysis Nonconformance.)

F. OPERATOR ACTION:

After review of this Westinghouse correspondence, Reactor Engineering and Analysis personnel notified Operations supervision, who notified the Control Room operators. The NRC Resident was notified at this time. At approximately 1540 EST on February 22, 1999, plant staff determined that a non-emergency one hour notification, per 10CFR50.72 (b) (1) (ii) (B), should be made to the NRC Operations Center. The Shift Supervisor made this notification at approximately 1601 EST on February 22, 1999.

Operators maintained a restriction of 40 degrees Fahrenheit maximum on screenhouse bay temperature from the time of discovery until plant shutdown on March 1 to ensure adequate margin existed.

G. SAFETY SYSTEM RESPONSES:

None

III. CAUSE OF EVENT:

A. IMMEDIATE CAUSE:

The immediate cause of the plant being in a condition that was outside the design basis of the plant was deficiencies in the Westinghouse MSLB mass and energy release analysis.

B. ROOT CAUSE:

The underlying cause of the deficiencies in the Westinghouse analysis was the analysis did not account for a greater volume of high temperature feedwater and used an incorrect feedwater isolation time. The additional mass and energy release from the MSLB are penalties in the containment pressure calculation.

IV. ANALYSIS OF EVENT:

This event is reportable in accordance with 10 CFR 21 and in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (ii) (B), which requires a report of, "Any event or condition ... that resulted in the nuclear power plant being ... In a condition that was outside the design basis of the plant".

An assessment will be performed considering both the safety consequences and implications of this event. A supplement to this LER will be submitted with the results of this assessment. The following are results and conclusions of a preliminary assessment:

There were no operational or safety consequences or implications attributed to the deficiencies in the Westinghouse MSLB mass and energy release analysis because:

The MSLB containment analysis is presented in Ginna Station UFSAR Section 6.2.1.2.3. A revised analysis was performed by offsetting the adverse effects of the additional mass and energy release through refinements in the existing analysis assumptions. These improvements do not alter the total quantity of steam released to containment, but provide benefits in lowering the rate of the release and increasing the rate of containment heat removal. Applying these analysis improvements to the MFRV failure cases initiated from 70% power (approximate power level at time of discovery) yields peak containment pressures that are less than those calculated in 1995.

The current Westinghouse analysis shows that the peak containment pressure design basis value of 60 psig would not be exceeded provided that service water (SW) temperature (SW supplies the containment recirculation fans) is limited to less than 45 degrees Fahrenheit. Prior to entering Mode 4 for the planned 1999 refueling outage, the screenhouse bay temperature was being maintained at approximately 39 degrees Fahrenheit, while lake temperature was approximately 35 degrees Fahrenheit. Thus, plant operation remained within its design basis since the time of discovery.

Any small increase in containment pressure beyond the 60 psig design basis value would not be expected to fail the containment. In 1996, the containment was successfully tested to 72 psig during the Structural Integrity Test for the steam generator replacement project. A steam line break does not result in severe radiological consequences at Ginna Station; thus full containment integrity is not considered required for this event (even though containment isolation is assumed to occur).

V. CORRECTIVE ACTION:

A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

For the operation of Ginna Station between the time of discovery and plant shutdown on March 1, 1999, the screenhouse bay temperature was maintained at approximately 39 degrees Fahrenheit, while lake temperature has remained at approximately 35 degrees Fahrenheit. Thus, plant operation remained within its design basis since the discovery date.

Ginna Station placed a temporary administrative restriction of 40 degrees Fahrenheit maximum on screenhouse bay temperature for Modes 1 through 4 (when containment is required to be operable) to ensure adequate margin existed.

B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

Additional analyses are being performed to support future cycle operation. Results of these analyses will be provided in a supplement to this LER. During the shutdown, RG&E is working closely with Westinghouse to resolve this issue.

The reactivity feedback in the analysis will be examined more closely to determine whether there is a return to power after the postulated MSLB in future cycles of operation. If necessary, the Ginna Station Core Operating Limits Report (COLR) will be changed to reflect more conservative shutdown margin levels.

Additional corrective actions, if needed, will be identified in a supplement to this LER.

VI. ADDITIONAL INFORMATION:

A. FAILED COMPONENTS:

None

B. PREVIOUS LERs ON SIMILAR EVENTS:

A similar LER historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.

C. SPECIAL COMMENTS:

None


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